Brian and Paige were
engaged while we were down there, and we're now looking forward to a May
wedding .
The boat was a Gibsea 51
- 27 tons - and incredibly stable. We were out in some pretty stiff breezes
and only rarely were we able to get any water actually flowing over the
rail. It seems quite a bit more stable than the beneteau 50 we had last time
we had the rail in the water on a regular basis. The boat had a decent
speed - making mile after mile at over 9 kts, with a top speed (that we saw)
of 10.2 on a reach.
All lines were lead back
to the cockpit, and all winches were self tailing. One thing we missed on
this trip was the electric winch we had on the beneteau. It wasn't a big
deal - but it really did make a difference when hoisting the main.
We had no "real"
problems with the boat except that the engine kill switch failed on the
second day out, and we ran out of water unexpectedly when the water pump was
unable to draw a suction on one of the four water tanks.
We pulled into the
Sunsail docks one day as we were passing by - to top off the water tanks,
and sunsail offered to fix the water issue and the engine kill switch, but
it wasn't a big deal since the water tanks were now topped off - and we were
able to kill the engine manually. We simply removed an engine access cover
in the aft-stbd cabin and manually tripped the fuel racks.
For the trapeze stuff we
were expecting we'd be able to use an extra halyard - but not so. We
improvised by removing the boom topping lift once we were underway - then
using the topping lift for our makeshift halyard. It was perfect.
The initial plans had us
turning the boat in on Saturday, then everyone flying back on Monday, but 3
days prior to our departure, Delta cancelled all Monday flights. As a
result, half of us flew back on Sunday, and the other half spent another 5
days there, returning the following Friday. We had GREAT rooms on a bluff,
overlooking the ocean - a perfect setting.